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#1 |
Registered Member
Join Date: Mar 2004
Location: Long Island
Posts: 58
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![]() My head gasket blew, i took the job on by my self to change my head gaskets.
when putting my 1.6 svo rockers back on, i notice one of the rockers still have alot of play in it, even though the bolt is tight! i thought maybe bent pushrod, so i swiched it over w/ rocker next door. STILL alittle play, not a crazy amout though, not enough play for the push rod to come out of the rocker socket or anything but loose enough that can wiggle it alittle. so i kept if moving w/my repair putting the motor back together, when i started the car a heard a crazy amout of rakcet going on , but i waited for the lifters to fill w/oil and it quited down alot , but theres a crazy loud TICK ! im guessing it that rocker that had play... why would that rocker have play when the rocker bolt if tightend till i can screw it down anymore ? ? ? someone told me i messed up a camlobe, but i thing my push rod would of bent before that would happen... please help
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1990 Mustang GT Engine- 308 (bored .40 over) Probe Forged pistons (10.5:1), Scat forged crank and rods, w/Main Girdle, AFR 185 heads, GT-40 intake, CSI electric water pump. AC delete kit, No smog pump, Manual rack and pinion steering. Ignition- MSD 6AL, MSD Blaster coil, MSD hellicore wires. Drive Train- Tremic 3550, Alum. Drive shaft, 3:73 gears, Stock carrier and axels. 26X11.5 M/T Et streets. Power adder- 175 shot of laughing gas. Best ET 11.5 @120mph on squeeze, 12.4 @109mph on muscle (on gt40 heads) on the 185 heads ... ??? tba |
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#2 |
Registered Member
Join Date: Nov 1998
Location: Houston, Tx.
Posts: 3,887
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![]() Could be a bad lifter? Did you switch the push rod when you did the lifter? Still could be a bent puish rod.
Rev
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'66 Coupe, 306, 350-375 HP, C-4, 13.07 e.t., 104.8 mph, 1/4 mi. O.B.C. #2 '66 coupe |
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#3 |
Registered Member
Join Date: Jun 2003
Location: Wisconsin
Posts: 348
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![]() I'd guess you had a collapsed lifter.
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92 Mustang GT, 347 Stroker(Forged Steel Crank/Rods-Balanced, Forged Aluminum Dished Pistons), Trick Flow Track Heat Intake, Trick Flow Twisted Wedge Heads w/ Stage 3 port/polish, 80mm C&L MAF, FMS 30# Inj., BBK AFPR, Trick Flow Stage 2 Cam, Trick Flow 1.6R Rockers, BBK E.L. Headers, Flowmaster Cat-Back, MAC CAI, FMS Pulleys, Griffin Alum. Radiator, MSD Pro-Billet Distributor; AOD, Dynamic 3300 Lockup Converter, B & M Super Cooler, B&M Ratchet Shifter; 3:73 gears. |
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#4 |
Registered Member
Join Date: Mar 2004
Location: Long Island
Posts: 58
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![]() i switched push rods around w/ 3 different ones, and i changed the lifter on the valve too !! any other ideas ?
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1990 Mustang GT Engine- 308 (bored .40 over) Probe Forged pistons (10.5:1), Scat forged crank and rods, w/Main Girdle, AFR 185 heads, GT-40 intake, CSI electric water pump. AC delete kit, No smog pump, Manual rack and pinion steering. Ignition- MSD 6AL, MSD Blaster coil, MSD hellicore wires. Drive Train- Tremic 3550, Alum. Drive shaft, 3:73 gears, Stock carrier and axels. 26X11.5 M/T Et streets. Power adder- 175 shot of laughing gas. Best ET 11.5 @120mph on squeeze, 12.4 @109mph on muscle (on gt40 heads) on the 185 heads ... ??? tba |
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#5 |
Registered Member
Join Date: Nov 1998
Location: Houston, Tx.
Posts: 3,887
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![]() If it was a bad lifter and you just switched it then it would have just transferred the problem to another valve. Did the play in the valve train stay at the same original valve that was causing the problem after ytou switched the components?
Rev
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'66 Coupe, 306, 350-375 HP, C-4, 13.07 e.t., 104.8 mph, 1/4 mi. O.B.C. #2 '66 coupe |
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#6 |
Registered Member
Join Date: Sep 2002
Location: Boston
Posts: 592
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![]() I heard an intense ticking coming from my engine and I assumed that the valvetrain was on it's way out. One day, while spelunking in the enginebay, I decided just for laughs to tighten the header bolts. VIOLA! No more ticking. Miniscule exhaust leaks in the header area sound like ticking. Give it a shot, cant hurt
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91 GT Carb conversion, holley 600 double pumper, edelbrock performer intake, FMS "C" drop springs, march 1000 underdrive pullies, crane 1.7 roller rockers, GT-40P headers, bassani x pipe, american thunder catback, FMS 4.56's, msd aL6, trunkmount battery, A/C eliminator kit, 3000 stall tci streetfighter, AOD with transgo kit, A+ servo, 300M hardened lockup shaft, kevlar bands and 28,000 gvw trans cooler, 3 core radiator, 300 lbs stripped with a full interior |
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#7 |
Registered Member
Join Date: Nov 1998
Location: Houston, Tx.
Posts: 3,887
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![]() A leaking header does sound just like a loose valve adjustment or a bad lifter. But didn't he say there was play in the valve train for one valve?
Rev
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'66 Coupe, 306, 350-375 HP, C-4, 13.07 e.t., 104.8 mph, 1/4 mi. O.B.C. #2 '66 coupe |
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#8 |
I'd rather be basketweaving
Join Date: Feb 2000
Location: Indianapolis
Posts: 2,551
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![]() just to make sure, you ARE torquing the rockers down to the correct spec while it is on the basecircle of the cam? (both valves closed)
Did it possibly have shims in it before that may have fallen out before you put it back together?
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NMRA O/C 9516 NA pumpgas stickshift 347 10.65@125.6, 6.73@100, 1.41 60ft |
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