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#1 |
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Join Date: Apr 1999
Location: Seattle, WA, US
Posts: 33
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![]() Tackling the next problem on the car. The heater/defroster blower swith only works on the low speed. Is it the motor or the switch I will need to replace?
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Don 1971 Mach 1 351C/4sp |
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#2 |
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Join Date: Jul 2002
Location: Oklahoma City
Posts: 208
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![]() Most likely culprit is your heater resistor. The way your heater fan works is thusly:
power is applied to the switch, switch selects high, med, or low speed. High is a direct connection to the motor, med is a low resistance between the switch and the motor and low is a high resistance between the switch and the motor. On early cars the resistor is on the front of the heater box, don't know where it is located on a '71 but follow the switch wires and it will lead right to the resistor block. Replace the resistor and you should have all three speeds back. Note after removing the resistor you will see the elements burned out. This could have occurred from a motor near failure. I would take the fan motor out and have it checked by a motor shop to make sure its not running excess current. |
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#3 |
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Join Date: Apr 1999
Location: Seattle, WA, US
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![]() Who carry the new resistor? I noticed John's Mustangs listed the part not in stock and checked a few other suppliers without luck.
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Don 1971 Mach 1 351C/4sp |
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#4 |
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Join Date: Apr 1999
Location: Seattle, WA, US
Posts: 33
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![]() Took out the resistor and tested it with my ohm meter. Got a different reading on each prong (4.5, 2.3 and 1.5). I'm going to assume the resistor is fine and check the switch. I'm not crazy about taking out the heater unit to get to the motor. Since the motor works on 1 speed, you think it's the switch.
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Don 1971 Mach 1 351C/4sp |
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#5 |
Registered Member
Join Date: Jul 2002
Location: Oklahoma City
Posts: 208
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![]() Likely. Try this: remove the umbilical from the resistor so just the prongs are showing. Jumper 12 volts to each one of the prongs in turn. Fan should run at high, medium, and low speed. If this works, then switch is likely bad...problem can only be in the umbilical or switch.
Note: do not try this on other model year Mustangs. Some require power to be connected to the resistor and some require ground to be connected depending on year model. According to a schematic I have, your's requires 12 volts to be applied. Hold 12 volts on tab only long enough to hear motor speed up. If it doesn't speed up immediately, then remove jumper immediately. |
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#6 |
Registered Member
Join Date: Apr 1999
Location: Seattle, WA, US
Posts: 33
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![]() Ok, ran the test as suggested. Motor and resistor working as expected. I tried the ohm test on the switch and only 1 speed is available. Is there a switch replacement available or do I need to visit the wrecking yard?
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Don 1971 Mach 1 351C/4sp |
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#7 |
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Join Date: Mar 1999
Location: Ventura, California
Posts: 8,981
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![]() Sounds like you've got a handle on this, but i just wanted to mention that it's been my experience that when the fan only works on high, that the resistor is bad. Any other combination of speeds not working is almost always the switch.
![]() Take care, ~Chris
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#8 | |
Registered Member
Join Date: Jul 2002
Location: Oklahoma City
Posts: 208
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#9 |
Registered Member
Join Date: Apr 1999
Location: Seattle, WA, US
Posts: 33
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![]() I noticed you can take the switch apart by removing the back cover by bending the little prongs. Not sure once inside anything can be done. I won't go there until someone had attempted this and suceeded. Since I have one speed, I can live with it. In the meantime I will visit the wrecking yards. oh fun.....
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Don 1971 Mach 1 351C/4sp |
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#10 |
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Join Date: Jul 2002
Location: Oklahoma City
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![]() I tried this on my '65 two-speed fan motor switch and it failed although I have been successful at repairing switches like this in the past. Success depends on how badly the contacts have been pitted by past switch actions. Even if you are successful at repair you should look for a new one since expected life of a repaired switch is short.
Note that the switch for '66 has the same three positions and you might be able to adapt the '66 switch to your application. NAPA also has dozens of switches in their catalog with descriptions. Its possible you could find a suitable alternate switch. |
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#11 |
Registered Member
Join Date: Apr 1999
Location: Seattle, WA, US
Posts: 33
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![]() Took the switch apart and boy, there was so much gunk (years of dust mixed with ??) on the contacts. Cleaned them, put it back to tegether and working like new.
![]() Thanks for the troubleshooting tips.
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Don 1971 Mach 1 351C/4sp |
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#12 | |
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Join Date: Jul 2002
Location: Oklahoma City
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![]() Quote:
Good to hear your repair was successful. Happy Mustanging! |
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