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Old 08-03-2001, 05:52 PM   #1
FdMust88
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Question Quick Fix ? Is There One?


Let me run down my mods first and maybe someone can answer my question.. I have a 91 LX with, MAC after-cat exhaust, BBK H-pipe (off-road), stock headers, MAC cold air induction fender mount kit, Edelbrock 70mm T.B. and EGR plate, Pro-M 75mm MAF Sensor, Kirban Adj. Fuel Press. Reg., everything else is pretty much stock except wires, plugs and things like that.. Here is my question, this week I installed the 70mm T.B. (I opened up the intake), fuel press. Reg. (set @ 42psi), 75mm MAF, and the H-pipe, and disconnected the battery for over 20 minutes. Why have I, what seems to be, lost some torque?? Is the exhaust to free flowing and the T.B. too big? I chose these components because I plan on adding a supercharger in the future.. Is there a quick fix too gain back some of my torque without removing any of my new parts... Any suggestions or comments would be great, thanks...
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Old 08-03-2001, 06:00 PM   #2
Chris_H
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To be honest I think your TB is too big for everything being pretty much stock. I added my 65mm about 3 months ago, and there really was no need for a bigger TB with my combo. But I did it for the same reason you did, future mods. I'd say go back to your stock Tb and see if that fixes your problem.

Chris

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1987 LX, rebuilt 306, Mac shorty headers 1 5/8, 2 1/2" Mac off road h-pipe, 2 1/2" 2 Chamber Flowmasters cat-back, Mac underdrive pullies, 65mm Throttle Body/Spacer, 3.55, K&N, Tremec 3550, King Cobra Clutch, Steeda Tri-Ax, Steeda Adj. Clutch Quadrant, Autometer gauges, White face gauges, blue silicone radiator hoses.
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Old 08-03-2001, 07:02 PM   #3
Mr 5 0
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Good advice from Chris_H.

Sometimes, 'future mods' need to be done all at once and this is probably one of those times, at least as far as the TB goes.

As Chris said; try re-installing the stock TB, that should fix your low-end torque problem.
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Old 08-03-2001, 07:55 PM   #4
dinomite
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the tb, in conjunction with the open exhaust is the problem. putting your stock tb back on should help.

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Old 08-04-2001, 09:29 AM   #5
FdMust88
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Thanks Guys, I'll give it a try once I get some new gaskets. The old ones ripped apart when I removed the stock T.B.
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Old 08-04-2001, 01:13 PM   #6
SHaFT7
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the 70mm TB has a slower velocity than the 65mm TB does i believe, which means you're getting less air into the chambers

use a 70mm if you're using a blower or turbos

*i know i have a 70mm on mine, but the kid that had it b4 me put it on, and i don't have the money to do a 65mm*

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Old 08-04-2001, 02:22 PM   #7
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I agree, that 70 is too big. You exhaust isn't hurting you a bit though, now if you added 1 5/8 headers to a stock engine.... that would hurt your tq as well.

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