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Old 08-09-2004, 09:07 AM   #1
leathal injection
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Angry Ran 11.53 down the track ! now i hear aloud ticking!

i went to the track yesterday, ran 11.53 @120 mph. as soon as i drove around to pick my slip up , noticed my cars ticking pretty loud and hesitating, and when i give alil gas sometimes it sounds like its gotta slight backfire.
1st thing i thought was a bent pushrod, as soon as a got home i checked them out , there all straight! witch really didnt surprise me cause i just reaplaced them 6 months ago (with hardened pushrods) ..... what could it be, collapsed lifter ? bent valve ? any ideas ?

ifs it a bent valve, i think im gonna trash my GT40 P's and get new heads... How does the edel RPM performer 2.02 heads, perform against a pair of AFR 185's ?? please help ...

Thanks guys.
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1990 Mustang GT

Engine- 308 (bored .40 over) Probe Forged pistons (10.5:1), Scat forged crank and rods, w/Main Girdle, AFR 185 heads, GT-40 intake, CSI electric water pump. AC delete kit, No smog pump, Manual rack and pinion steering.

Ignition- MSD 6AL, MSD Blaster coil, MSD hellicore wires.

Drive Train- Tremic 3550, Alum. Drive shaft, 3:73 gears, Stock carrier and axels. 26X11.5 M/T Et streets.

Power adder- 175 shot of laughing gas.

Best ET 11.5 @120mph on squeeze, 12.4 @109mph on muscle (on gt40 heads)

on the 185 heads ... ??? tba
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Old 08-09-2004, 10:30 AM   #2
~The Jester~
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Sounds like you're barking up the right tree at least. Ticking is probably a lifter, and the running crappy and minor backfire is probably a burned valve, not necessarily bent but could be. Run a compression test, and that'll let you know where the problem is.

Good luck!
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Old 08-09-2004, 11:22 AM   #3
leathal injection
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ok , i went and bought a compression tester...

i take the #5 spark plug out and its TOTALLY MELTED !!! i ran the compression test on that cylinder anf there NO compression in that cylinder.
i thought maybe i bought a busted tester , but it shows compression on other cylinders ! im taking it apart now, i hopes there isnt a huge hole in my piston !
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1990 Mustang GT

Engine- 308 (bored .40 over) Probe Forged pistons (10.5:1), Scat forged crank and rods, w/Main Girdle, AFR 185 heads, GT-40 intake, CSI electric water pump. AC delete kit, No smog pump, Manual rack and pinion steering.

Ignition- MSD 6AL, MSD Blaster coil, MSD hellicore wires.

Drive Train- Tremic 3550, Alum. Drive shaft, 3:73 gears, Stock carrier and axels. 26X11.5 M/T Et streets.

Power adder- 175 shot of laughing gas.

Best ET 11.5 @120mph on squeeze, 12.4 @109mph on muscle (on gt40 heads)

on the 185 heads ... ??? tba
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Old 08-09-2004, 02:33 PM   #4
88fivepointoh
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Thats Harsh, I am going to bet on a bent valve... well now you have an excuse for the heads.
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Old 08-10-2004, 05:59 PM   #5
MiracleMax
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how bout a burnt piston? , is there real bad blowby? Although the backfire does suggest a bad valve.
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Old 08-10-2004, 06:49 PM   #6
leathal injection
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i took the head off and the there is a hole in my exhuast valve. the piston looks pretty good. im going to get new heads today. im thinkin about the edel Rpm Performer heads w/2.02 intake valves ? how good are these heads over my gt40-p's ?
__________________
1990 Mustang GT

Engine- 308 (bored .40 over) Probe Forged pistons (10.5:1), Scat forged crank and rods, w/Main Girdle, AFR 185 heads, GT-40 intake, CSI electric water pump. AC delete kit, No smog pump, Manual rack and pinion steering.

Ignition- MSD 6AL, MSD Blaster coil, MSD hellicore wires.

Drive Train- Tremic 3550, Alum. Drive shaft, 3:73 gears, Stock carrier and axels. 26X11.5 M/T Et streets.

Power adder- 175 shot of laughing gas.

Best ET 11.5 @120mph on squeeze, 12.4 @109mph on muscle (on gt40 heads)

on the 185 heads ... ??? tba
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Old 08-10-2004, 07:02 PM   #7
88fivepointoh
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pop-ed a hole in there.. damn... edel brocks are good, trickflows, afr, etc.. everyone has there own flavor, I like them both.
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