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			 Registered Member 
			
			
		
			
				
			
			
			Join Date: Oct 1998 
				Location: Suburban Chicago, Hanover Park 
				
				
					Posts: 695
				 
				
				
				
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			 Finally got a couple runs in with the nitrous. Had mucho problems getting it to work right. First the bleeder hole that feeds nitrous up to the fpr was cloged and I was shooting straight nitrous, with no fuel 
		
	
		
		
		
		
		
		
			  I only picked up 2 tenths and 2mph and it took me about a few weeks to figure that one out. Finally got a schematic from ZEX and found that problem. Then I was popping and bucking the next trip to the track on the nitrous, but my fp gauge was broke, so I couldn't figure out where my fuel was at. Finally got that straightened out and made this run. Check out the 60', my previous best had been a 1.711. R/T .856 (I know, it sucks) 60' 1.597 330' 4.929 1/8 7.696 mph 88.02 1000 10.059 1/4 12.046 mph 113.62 My best time on motor so far is 12.9 @ 107. This 12.04 was also done into a 15-20mph headwind, so I'm sure I can get well into the 11's with some tuning. I'm just glad I could get the nitrous working before all the tracks shut down this year, if I get to go again, I'll be gunning for the 11's ![]() 
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	My Ford Club http://www.midwestfords.org/ Best time N/A 12.9 @ 107 1.711 60' 125 shot - 12.04 @ 113 1.59 60'  | 
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			Join Date: Jun 2002 
				Location: Nebraska 
				
				
					Posts: 127
				 
				
				
				
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			 nice job! I wish i could run 12's......... 
		
	
		
		
		
		
		
		
			
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	1988 Mustang 5.0 LX Convertible -Mac Cold Air Intake -K&N Cone Filter -9mm FMS Spark Plug Wires -Hedmann Headers 2.5" O/R H-Pipe -Flowmaster 40 series 2.5" Catback  
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			 I'd rather be basketweaving 
			
			
		
			
				
			
			
			Join Date: Feb 2000 
				Location: Indianapolis 
				
				
					Posts: 2,551
				 
				
				
				
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			 awesome times man. Was it up at US41? 
		
	
		
		
		
		
		
		
			How big of a "shot" are you running with that Zex kit? I still haven't had a good chance to try out the nitrous in my car, and I know it will go 11's with the 100shot on a good day. But the current combo is goin out the window, and I'm gonna try for low 12's NA and mid 11's on a 125shot next season. We should plan an early spring mustang day up at US41, I'll definately be needing to smell some burning tires by then ![]() 
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	NMRA O/C 9516 NA pumpgas stickshift 347 10.65@125.6, 6.73@100, 1.41 60ft  | 
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			 Registered Member 
			
			
		
			
				
			
			
			Join Date: Oct 1998 
				Location: Suburban Chicago, Hanover Park 
				
				
					Posts: 695
				 
				
				
				
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			 Quote: 
	
 I'm running the 125 shot. 
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	My Ford Club http://www.midwestfords.org/ Best time N/A 12.9 @ 107 1.711 60' 125 shot - 12.04 @ 113 1.59 60'  | 
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			 Registered Member 
			
			
		
			
				
			
			
			Join Date: Oct 1999 
				Location: Pierre Part, La. U.S.A. 
				
				
					Posts: 1,850
				 
				
				
				
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			 CONGRADULATIONS DUDE!  I will run mine Wed. I now have a third gear. I also had to weld the too top ears back on the tremac. These were broke due to a bad (very bad) tranny mount. I put all poly mounts and bushings also, and welded the torque box that a friend of mine welded up and I never inspected. Cause it was still broke. I ran 12.22 @ 111 with out third gear. I can not wait to see if I can break 11s also. 
		
	
		
		
		
		
		
		
			
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	88workcar 1988 Mustang LX 342. 417rwhp @ 6800. 28 X 10 ET Drag, 4.30s, 10.69 @ 126.43 1.42 60ft. 11.13 @ 127.7 on BFGs 1.72 60ft Rice Hater # 42 To be old and wise, You must first be young and stupid   I'm somewhere in tthe middle.
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