Blown Motor...
Alright for those of you who dont know The motor in my car blew a week ago today.. i finally pulled everything out over the past week and found out what it is... my intake valve on the #1 cylender is in 4 peices... the valve broke around the groove for the retainer letting the valve fall into the cylender and, well gues what happenced from there... a peice of the valve steam about a 1/2inche long is completely imbeded in the piston... the piston is copletely cracked and seized in the block...
SOO, i am looking at a new short block and new set of heads (fairly stock) i cant spend alot of cash ill do heads later...
I was looking at either a 306-317 block who makes a good one.. and for around $1200-$1600 for the short block...
If Any one has a set of OK E-7 heads htat can be rebuilt ill see what i can do to take them off your hands
IF any one has any good INFO I would love it... OHH i dont think i can race a carlsbad... so i think i am going to do my 5 minute doccumentry for my Broadcasting class for collage, at the race way...
------------------
PPG Torch Red 95GT, Ported Explorer Intake, E-303 cam, 75mm MAS, BBK Adj. fuel Reg & gauge, BBK Shorty Headers, BBK H-pipe, March Pulleys, 2 Chamber Flowmasters, Kenny Brown 6 point Roll cage, Kenny Brown Panhard Bar, Powerslot Rotors, Eibach Sportline Springs, 180* Thermostat, 1/2 Plenum Spacer, MSD 6AL, MSD Master Blaster, MSD 8.8 Wires, 19# Racing Injectors, AFS 10.5" Cobra R's, Nitto 555's, Eclipse & JL Stereo System... I just sold My K&N, It looks funny with Stock Air Box & filter!!!
|