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-   -   Quick Fix ? Is There One? (http://forums.mustangworks.com/showthread.php?t=4945)

FdMust88 08-03-2001 05:52 PM

Quick Fix ? Is There One?
 

Let me run down my mods first and maybe someone can answer my question.. I have a 91 LX with, MAC after-cat exhaust, BBK H-pipe (off-road), stock headers, MAC cold air induction fender mount kit, Edelbrock 70mm T.B. and EGR plate, Pro-M 75mm MAF Sensor, Kirban Adj. Fuel Press. Reg., everything else is pretty much stock except wires, plugs and things like that.. Here is my question, this week I installed the 70mm T.B. (I opened up the intake), fuel press. Reg. (set @ 42psi), 75mm MAF, and the H-pipe, and disconnected the battery for over 20 minutes. Why have I, what seems to be, lost some torque?? Is the exhaust to free flowing and the T.B. too big? I chose these components because I plan on adding a supercharger in the future.. Is there a quick fix too gain back some of my torque without removing any of my new parts... Any suggestions or comments would be great, thanks...

Chris_H 08-03-2001 06:00 PM

To be honest I think your TB is too big for everything being pretty much stock. I added my 65mm about 3 months ago, and there really was no need for a bigger TB with my combo. But I did it for the same reason you did, future mods. I'd say go back to your stock Tb and see if that fixes your problem.

Chris

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1987 LX, rebuilt 306, Mac shorty headers 1 5/8, 2 1/2" Mac off road h-pipe, 2 1/2" 2 Chamber Flowmasters cat-back, Mac underdrive pullies, 65mm Throttle Body/Spacer, 3.55, K&N, Tremec 3550, King Cobra Clutch, Steeda Tri-Ax, Steeda Adj. Clutch Quadrant, Autometer gauges, White face gauges, blue silicone radiator hoses.
Best times:
2.331 60ft, 9.966 @ 71.069 1/8 mile, 15.491 @ 91.846 1/4 mile at 4000 ft. elevation on street tires
207.0 RWHP 279.7 RWTQ

Mr 5 0 08-03-2001 07:02 PM

Good advice from Chris_H.

Sometimes, 'future mods' need to be done all at once and this is probably one of those times, at least as far as the TB goes.

As Chris said; try re-installing the stock TB, that should fix your low-end torque problem.

dinomite 08-03-2001 07:55 PM

the tb, in conjunction with the open exhaust is the problem. putting your stock tb back on should help.

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90LX AOD Convertable: Lakewood control arms, FMS springs.
Best 1/4: 15.277@92.25 (2.27 60')
AIM: dinomite1, roadracestang
dinomite@softhome.net

FdMust88 08-04-2001 09:29 AM

Thanks Guys, I'll give it a try once I get some new gaskets. The old ones ripped apart when I removed the stock T.B.

SHaFT7 08-04-2001 01:13 PM

the 70mm TB has a slower velocity than the 65mm TB does i believe, which means you're getting less air into the chambers

use a 70mm if you're using a blower or turbos

*i know i have a 70mm on mine, but the kid that had it b4 me put it on, and i don't have the money to do a 65mm*

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SHaFTed

91GT, 2 chamber flows, dumps, 70MM BBK TB, K&N conical, Robert Shaw tstat, Hurst short throw, T5, 17" Lexani Roma wheels, 235/40/R17 on front, 255/45/R17 on back, mach1 hood, LX tail lights, bright red!

rbatson 08-04-2001 02:22 PM

I agree, that 70 is too big. You exhaust isn't hurting you a bit though, now if you added 1 5/8 headers to a stock engine.... that would hurt your tq as well.

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Rick
My 89lx(updated 7/20/2001)
Sold:(


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