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#1 |
Registered Member
Join Date: Oct 2005
Posts: 3
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![]() Hi all, I need help to find out some info with my 1995 mustang engine, (stock standard, curved intake neck). Firstly need to know what the IAC (Idol Air Control) screw looks like. I know where it is supposed to be... as I have removed the grey rubber plug on the throttle body and there is just a hole with a thread inside.... NO adjustment screw in there at all!! I was told by the guy who tuned the engine that "maybe it came loose in the throttle body and was sucked into the intake" this sounds to me like a whole lot of BULL SH!T, however I am led to ask the question is this possible?.
I need to know because the engine now has a misfire on number 2 cyl. The engine had just been dyno'd by this guy and he said that is was running perfectly fine on the dyno. Now I have a missing number 2 cyl, and he is claiming it is not his problem. He performed a leak-down test and discovered air leaking back into the intake... which indicates the intake valve is not seating. Symptoms when running: -Cold exhaust temp on number 2cyl -Can easily hear the misfire on the right bank (twin exhaust system) -good fuel inj, spark/leads, dizzy cap, coil What could have caused my engine to now be running on 7 cylinders??? The day I picked the car up there was this problem with it. Is it possible that the IAC screw has gone through the engine and damaged the intake on number 2cyl? Please... any help on this will be appreciated, Simmo Last edited by simon clemens; 10-12-2005 at 08:28 AM.. |
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#2 |
Rearview Mirror Haze
Join Date: May 1999
Location: Huntsville, Alabama...a.k.a. "HuntsVegas"
Posts: 387
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![]() If you've changed the plug, wire, cap, button... it seems to me you want to get the computer checked for an error code and if that doesn't tell you anything, tear the top of that motor down.
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93 lx Notch 01 GT ![]() ...the epitome of Murphy's Law |
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#3 |
Moderator
Join Date: Sep 1998
Location: Grand Rapids, Michigan, USA
Posts: 1,001
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![]() If it is the case that a screw was sucked into the #2 intake runner, and from your description, then maybe you got really lucky and it's just jamming the intake valve open, thus no compression on that cylinder. I would at least take the upper intake off and see if you can look down there. If not, remove the lower and be sure. Go from there. Good luck.
p.s. if this guy's so intent on it not being "his problem" i'd consider doing a lawnjob in his front yard not "your problem" ![]() ![]()
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Capri306, Moderator The Mustang Works Online 1979 Mercury Capri 1987 5.0L Mustang LX Notchback 1993 5.8L Eddie Bauer Bronco ![]() |
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#4 |
Registered Member
Join Date: Oct 2005
Posts: 3
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![]() Thanks for the replies fellas, will add to my post when i have found the problem... Believe me I've thought about doing worse things than a lawn job! He has really pushed the wrong buttons
![]() When I get it back from these idiots I'll do my own compression test, I just don't trust that they know what their doing, may still have to pull the head off, its not a big job, just extra unwanted hassle Simmo... |
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