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12-01-2001, 06:03 PM | #1 |
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Join Date: May 2001
Location: Valdese, NC
Posts: 361
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White smoke and antifreeze smell!
Yes you guessed it, headgasket. I changed plugs and put new plug wires on my car last week. A friend helped as I didn't have the necessary tools to get in under the turbo. I left it there for him to finish as I had some where to go. When I drove it home I noticed it running a little hotter than normal. I didn't drive it for a few days, but when I did it smoked something awful.
I've had some problems with overheating for a while but they come and go. My turbo also has some signs of wear and I've seen white smoke from time to time, but reving it up always clears it out. I took it out this morning and sure enough there was the smoke again. It also ran a little hotter than normal. I called the guy that tunes for me and he said to bring it over. I left it there for him to begin tearing it down, although it's going to be a couple of weeks before he can get to it. It was about to be put up for winter anyway. Ansuming my luck isn't completely bad and it's nothing like a craked block. I'm going to put dart jrs, a larger down pipe, new larger headers, new 60-1 turbo, and an adjustable boost control on it. I've got to call Turbo Tech about the larger down pipe, but hopefully everything will go well.
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91 single turbo vert |
12-01-2001, 06:14 PM | #2 |
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Join Date: Mar 1999
Location: Arcadia, CA, USA
Posts: 731
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Hey, sorry to hear that...I feel your pain, been there/done that. But like you said, blowing a head gasket is a lot easier to fix than a block or reciprocating assembly. I believe it's just fine to have the head gasket as the weakest link.
Suggest sorting out the cause of the blown head gasket if you haven't already. The last time mine blew was when the T-rex failed. Good luck with it.
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Russ L '91 LX - 331 w/ Procharger '03 Cobra Convertible - Pullied '94 Lightning '65 Mustang Coupe |
12-01-2001, 07:50 PM | #3 |
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Join Date: Feb 1999
Location: Utica, Michigan
Posts: 2,631
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Maybe your heads are now warped?
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1988 Mustang GT stock bottom 302, C4 10.9 @ 128 with 8 psi of Novi 1000 boost!----STOLEN 1989 Mustang notchback Warmed up 306 with a Procharger. |
12-01-2001, 09:37 PM | #4 | |
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Join Date: May 2001
Location: Valdese, NC
Posts: 361
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Quote:
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91 single turbo vert |
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12-01-2001, 10:39 PM | #5 | |
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Join Date: Apr 2001
Location: Bowling Green, OH
Posts: 270
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Quote:
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1989 lx notch 89,000 miles 5-speed, bolt-ons, 3.73, TFS TWs, TFS Track Heat, TFS Stage 1 cam |
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12-02-2001, 08:26 AM | #6 | |
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Join Date: May 2001
Location: Valdese, NC
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Quote:
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91 single turbo vert |
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12-02-2001, 10:31 AM | #7 |
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Join Date: Apr 2001
Location: Bowling Green, OH
Posts: 270
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What cam are you running?
Awhile back, I helped a guy put set of Srs (64cc w/ upgraded hardware) on with stock pistons and an E-303 cam, without any problems. But like you said, you have had good luck with the jrs in the past, so go with what you think works best. Are you going to buy them bare and have good hardware installed?
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1989 lx notch 89,000 miles 5-speed, bolt-ons, 3.73, TFS TWs, TFS Track Heat, TFS Stage 1 cam |
12-02-2001, 01:02 PM | #8 | |
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Join Date: May 2001
Location: Valdese, NC
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Quote:
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91 single turbo vert |
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