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				 Success!!! 
 Classic Lean misfire? Well, it cost me about 30hp at the dyno.
 I checked/replaced:
 plugs
 wires
 cap
 rotor
 TFI(2x)
 timing (4x)
 fuel pressure
 vacuum leaks
 fuel pump
 TPS
 ECT sensor
 ACT sensor
 
 any guesses?
 How about the "Hall Sensor" INSIDE the distribitor?
 It failed a resistance check after all of the aforementioned troubleshooting.
 So much for my fancy MALLORY Ignition. Do not but the Mallory distributor.
 I found my duraspark that has been sitting in a box for 4 years and it is the best my car has run with the new motor yet.
 
 Mustangs..if you have one, you are probably going to become a problem drinker. But you'll be a quick one.
 
				__________________1988 GT Convertible 
331 10:1 TW heads, GT-40 intake, MSD, TRW flattops, B Cam w/ 1.7's, MAC exhaust, 24's, 70 TB, 76 MAF, 3.73's, Pro 5.0, Koni's, Anderson PMS, Wideband 02, yatta, yatta... 
One week with new motor, two speeding tickets...joy
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