I did that and when i looked down in there it was all corroded and crap was covering the holes inside the radiator. I went and bought a cleaner and it said to drive it for 6 hours with that and water in it. I put that in and drove it for like 10 minutes. It is still running a little hotter than usual about 1 line highr on the gauge (in between the M and the A). After, I will drain it again and add this pure blend stuff that is supposed to lower the temp 28 degrees (yeah right). Any other suggestions after I run it for a few hours? Also, Im an idiot- I cant get the hose off thats above the thermostat to gain access to the bolts. any suggestions? Thanks for all replies- Just trying to save money and do this crap myself!
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90 lx hatch, holley systemax II kit, rebuilt 302, BBK 155 lph fuel pump, pro M bullet mass meter wtih BBk cold air intake, 30 # injectors, 70 mm TB, jacobs ignition system, edelbrock water pump, BBk longtube headers with h-pipe, flowmasters, b&m ripper shifter, 3.55 gears, Proform electric fan, subframe connectors/removed smog pump and ac!
75 shot of nitrous!
13.2 at 112 1/4 mile- no traction!
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