View Single Post
Old 01-27-2004, 12:59 AM   #7
Hozer 88GTConv
Registered Member
 
Hozer 88GTConv's Avatar
 
Join Date: Feb 2002
Location: Jacksonville, FL
Posts: 706
Default Test...

Well,
Things just aren't going well. I busted a o-ring on a fuel injector while replacing the intake manifold after the valve seal/guide troubleshoot. What a PITA.
No hint as to what is causing the prob. I know I must remove the heads now in order to finally see what is going on.
Best thing I can think of is a bad ring now. I'll post it when I find out.
Still amazing though, no freakin smoke.
Compression is within 5 percent on all cylinders including the known "bad" one, number 5.
__________________
1988 GT Convertible
331 10:1 TW heads, GT-40 intake, MSD, TRW flattops, B Cam w/ 1.7's, MAC exhaust, 24's, 70 TB, 76 MAF, 3.73's, Pro 5.0, Koni's, Anderson PMS, Wideband 02, yatta, yatta...
One week with new motor, two speeding tickets...joy
Hozer 88GTConv is offline   Reply With Quote