Test...
Well,
Things just aren't going well. I busted a o-ring on a fuel injector while replacing the intake manifold after the valve seal/guide troubleshoot. What a PITA.
No hint as to what is causing the prob. I know I must remove the heads now in order to finally see what is going on.
Best thing I can think of is a bad ring now. I'll post it when I find out.
Still amazing though, no freakin smoke.
Compression is within 5 percent on all cylinders including the known "bad" one, number 5.
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1988 GT Convertible
331 10:1 TW heads, GT-40 intake, MSD, TRW flattops, B Cam w/ 1.7's, MAC exhaust, 24's, 70 TB, 76 MAF, 3.73's, Pro 5.0, Koni's, Anderson PMS, Wideband 02, yatta, yatta...
One week with new motor, two speeding tickets...joy
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