Number 1...
You were absolutely correct.
Number one intake rocker arm was almost totally off.
I couldn't believe it. I checked all of them on the passenger side and the luck nuts were tight.
Hmm.
I checked the valves three complete times before re-installing the intake manifold.
I am wondering now since I only tightened the rocker nut 1/8-1/4 turn and then tightened the lock nut that they might back off.
Damn.
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1988 GT Convertible
331 10:1 TW heads, GT-40 intake, MSD, TRW flattops, B Cam w/ 1.7's, MAC exhaust, 24's, 70 TB, 76 MAF, 3.73's, Pro 5.0, Koni's, Anderson PMS, Wideband 02, yatta, yatta...
One week with new motor, two speeding tickets...joy
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