© Copyright 1995 thru 2008 - The Mustang Works™. All Rights Reserved.
MustangWorks.com is designed and hosted by Aero3 Media.
MustangWorks.com is designed and hosted by Aero3 Media.
10-22-2006, 11:42 PM | #1 |
Registered Member
Join Date: Sep 2000
Location: rock hill,S.C. 29730
Posts: 420
|
HELP disappointing time slips!!!!
Went to 1/8 mi. strip today.
15* timing 40-42# fuel pressure. Only went 9.00 @77.5 My old bolt-on stocker was faster. 8.75 @ 77.6 What's going on?? Tmoss said headers seemed big but It's got tons of tourqe, on the street it seems MUCH faster but 9.00's?? Granted my shifter was hanging up on me and I missed some shifts but on the 3 9.00's (all almost identical) I hit 2 & 3rd pretty good, not powershift fast, but smooth.60 ft's still 1.8-1.9
__________________
88 GT: subs,pullies, 1 3/4 longtubes, flowmasters, AFR 165's,T,F #1 cam,Thyphoon intake, 24# inj., 73mm C&L,65mmT.B., 190LPH pump, Eagle sir rods, forged pistons in a newly rebuilt 306. DYNO TUNED TO 300.97 RWHP 337RWTQ |
|
|
Similar Threads | ||||
Thread | Thread Starter | Forum | Replies | Last Post |
Back from the track....did worse than last time!! | 82 GT | Windsor Power | 18 | 05-12-2005 10:21 PM |
Long Time No Post | OnMy3rdStang | Blue Oval Lounge | 4 | 12-05-2004 10:34 PM |
My report from racing at the NMRA event in Bowling Green (was ATTN: Lt. Dan) | andy669 | Racer's Club House | 12 | 10-08-2003 02:41 PM |
Have not had race in a long time. | Five0 | Stang Stories | 2 | 12-23-2001 11:50 PM |
Towed away this time! (Long) | 1988GTCONERTIBLE | Windsor Power | 6 | 10-26-2001 06:05 PM |