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			 Registered Member 
			
			
		
			
				
			
			
			Join Date: Feb 2002 
				Location: Jacksonville, FL 
				
				
					Posts: 706
				 
				
				
				
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			 Classic Lean misfire?  
		
	
		
		
		
		
		
		
			Well, it cost me about 30hp at the dyno. I checked/replaced: plugs wires cap rotor TFI(2x) timing (4x) fuel pressure vacuum leaks fuel pump TPS ECT sensor ACT sensor any guesses? How about the "Hall Sensor" INSIDE the distribitor? It failed a resistance check after all of the aforementioned troubleshooting. So much for my fancy MALLORY Ignition. Do not but the Mallory distributor. I found my duraspark that has been sitting in a box for 4 years and it is the best my car has run with the new motor yet. Mustangs..if you have one, you are probably going to become a problem drinker. But you'll be a quick one. 
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	1988 GT Convertible 331 10:1 TW heads, GT-40 intake, MSD, TRW flattops, B Cam w/ 1.7's, MAC exhaust, 24's, 70 TB, 76 MAF, 3.73's, Pro 5.0, Koni's, Anderson PMS, Wideband 02, yatta, yatta... One week with new motor, two speeding tickets...joy  | 
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		#2 | 
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			 NX dealer-man 
			
			
		
			
			
			Join Date: Sep 1998 
				Location: Peoria, Illinois 
				
				
					Posts: 977
				 
				
				
				
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			 Excellent!  I am glad you've found your problem.  As far as the drinking goes, I'd be careful... 
		
	
		
		
		
		
		
		
			
		
		
		
		
		
		
	
	So what does that 30hp translate into for total RWHP? Did you make it to 340??? Later  | 
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		#3 | 
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			 He said Member...heh, heh 
			
			
		
			
				
			
			
			Join Date: Sep 1999 
				Location: Jupiter, Florida U.S.A. 
				
				
					Posts: 3,718
				 
				
				
				
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			 Cool, glad ya got it fixed, and now you won't have to worry about changing anything for a long time!  
		
	
		
		
		
		
		
		
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	Joe! 1988 GT, 13.58@101mph Check out my listing! Click here! Or my website:www.joe4speed.com  | 
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		#4 | 
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			 Registered Member 
			
			
		
			
				
			
			
			Join Date: Feb 2002 
				Location: Jacksonville, FL 
				
				
					Posts: 706
				 
				
				
				
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			 incidentally, I am putting in an SN 95 electric fan kit today as a little reward for discovering the problem.  
		
	
		
		
		
		
		
		
			It never ends... ![]() 
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	1988 GT Convertible 331 10:1 TW heads, GT-40 intake, MSD, TRW flattops, B Cam w/ 1.7's, MAC exhaust, 24's, 70 TB, 76 MAF, 3.73's, Pro 5.0, Koni's, Anderson PMS, Wideband 02, yatta, yatta... One week with new motor, two speeding tickets...joy  | 
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		#5 | 
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			 Registered Member 
			
			
		
			
				
			
			
			Join Date: Feb 1999 
				Location: Utica, Michigan 
				
				
					Posts: 2,631
				 
				
				
				
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			 Glad you got it worked out. I told you it was not the cam . 
		
	
		
		
		
		
		
		
		
		
		
	
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		#6 | 
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			 Registered Member 
			
			
		
			
				
			
			
			Join Date: Feb 2002 
				Location: Jacksonville, FL 
				
				
					Posts: 706
				 
				
				
				
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			 Exgmguy, 
		
	
		
		
		
		
		
		
			Me too. The fact that the motor had been missing since I installed everything had me thinking of at least the possibility of a "flat" spot on a lobe or something. I will probably still look into getting a custom grind after my next dyno run and see if it will yield some hp. I have a pretty tall hp order for my 306 by July. 
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	1988 GT Convertible 331 10:1 TW heads, GT-40 intake, MSD, TRW flattops, B Cam w/ 1.7's, MAC exhaust, 24's, 70 TB, 76 MAF, 3.73's, Pro 5.0, Koni's, Anderson PMS, Wideband 02, yatta, yatta... One week with new motor, two speeding tickets...joy  | 
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		#7 | 
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			 Registered Member 
			
			
		
			
			
			Join Date: May 1999 
				
				
				
					Posts: 5,246
				 
				
				
				
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			 I seem to remember somebody having problems with their Mallory distributor/ignition before, but I didn't want to jump the gun and point fingers.  At least you got the problem fixed, which is sweet. 
		
	
		
		
		
		
		
		
		
		
		
	
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		#8 | 
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			 Registered Member 
			
			
		
			
			
			Join Date: Mar 2002 
				Location: Rockingham,N.C. 
				
				
					Posts: 80
				 
				
				
				
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			 Congrats on the fix man ,can you tell me where to buy the sn-95 kit ?I had  a 95 GT and loved the fan setup over the clutch fan on my 88.I am upgrading to a 130 amp alt. so now it will be feasable to run a electric fan(damn underdrives lol) 
		
	
		
		
		
		
		
		
			
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	88 Notchback orig. 4 cylinder car with a efi v8 swap from a wrecked 89 5.0 hatch,edelbrock performer rpm's 190/160,typhoon intake,comp cams 1.6 rockers,65mm tb and spacer,pa performance c4 w/ 3000 stall,3.73's auburn pro, 31 spline mosers,mac off road h-pipe,1 5/8 shorties ,and 2 1/2 pro dumps,kirban fpr,190 lph walbrp. SOON TO BE BLOWN!  | 
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		#9 | 
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			 Registered Member 
			
			
		
			
				
			
			
			Join Date: Feb 2002 
				Location: Jacksonville, FL 
				
				
					Posts: 706
				 
				
				
				
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			 Racer Walsh here in Jacksonville 904-721-2289 
		
	
		
		
		
		
		
		
			email: http:/www.racerwalsh@ilnk.com #F5ZZ8C607A Electric Fan kit $221 and the 94-95 Fan Plug $20 They can get it quick. 1 day for mine. 
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	1988 GT Convertible 331 10:1 TW heads, GT-40 intake, MSD, TRW flattops, B Cam w/ 1.7's, MAC exhaust, 24's, 70 TB, 76 MAF, 3.73's, Pro 5.0, Koni's, Anderson PMS, Wideband 02, yatta, yatta... One week with new motor, two speeding tickets...joy  | 
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