
© Copyright 1995 thru 2008 - The Mustang Works™. All Rights Reserved.
MustangWorks.com is designed and hosted by Aero3 Media.
MustangWorks.com is designed and hosted by Aero3 Media.
|
|
#7 |
|
Registered Member
Join Date: Dec 1998
Location: WI, U.S
Posts: 255
|
I ran it today and it pulled strong like it usually does. I've been emailing with the guy I bought it from. I asked him if he had ever changed the fuel filter and I am waiting for a reply. He had mentioned checking all vacuum hoses and sensor connections. Everything looked good except for the positive and negative wire to the Blaster coil were loose enough I could undo the nuts with my finger. I tightened those done, took it for a spin and everything runs normal. I'll wait to see what he says about the fuel pump and filter. Thanks for your input!!
__________________
91 LX - 10.5:1 pistons, ported 289 heads, Ultradyne 588 cam, Cobra upper/lower, MSD, JBA long tube headers, Flowmaster, Richmond 4:10, roll cage, monster tach...FUN!! 95 SHO - K&N filter |
|
|
|
|
|
Similar Threads
|
||||
| Thread | Thread Starter | Forum | Replies | Last Post |
| Surging at higher speeds and RPM | Rosco | Windsor Power | 5 | 10-12-2003 11:08 PM |
| Surging / Bucking with SQ trim Vortech | NoPony | Power Adders | 2 | 07-12-2003 07:41 AM |
| surging problem? | speed_Freek170 | Small Ponies | 1 | 08-30-2001 11:58 AM |
| surging and idling problems | LXStallion | Windsor Power | 1 | 04-29-2001 12:27 AM |
| Idle problems & slight surging | Saleen308 | Windsor Power | 8 | 03-17-2001 07:21 PM |
