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Old 08-07-2004, 01:46 PM   #19
jimdrechsler
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Join Date: Apr 2001
Posts: 167
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This is what the final verdict is. good news. the crap i saw at the top of the fluid must of been corrision from the overflow tank. the car just doesnt seem as fast as it used to be, but it could be in my head. the smell must have been the antifreeze burning off the motor after it leaked a bit! her is waht my mechanic said:


i gave him 20 bux, he asked for 15 bux!


Based on Pressure checks Hot and Cold, could not find any major
problems(Intake Gkst, Head Gskt, cracked head..etc.) . As I noted I did find
leaks at Upper Hose at Thermostat, and By pass hose.
The one baffling item is there is a slight amount of water in the
oil. However it appears to have no anti-freeze in it. This is a good sign
since appears to be moisture(condensation) in the motor that settled out.
The oil did not appear "Milky" at all.
__________________
OLD CAR-89 lx convt- Flowtech II headers, H-pipe, 2 1/2 "flowmasters- pulleys- 3.73's, ripper shifter- ram air- Best 1/4 mile time- a measley 14.2 at 98.6

PRESENT CAR- 90 LX BBK long tubes, h-pipe with cats, flowmasters. 3.55's holley systemax II kit- 70 mm TB 30#injectors, jacobs ignition, black magic fan, 180 thermostat, 75 shot of NOS- NITTO DR'S

STREET TIRE BEST RUNS
1/4 mile13.2 @112 w/ NOS 2.17 60'
13.5 @103 2.1 60'

*new time with Dr's 12.8 at 111 w/ 75 shot
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