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#1 |
Ride Hard
Join Date: Oct 2000
Location: Wyoming IL
Posts: 1,094
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![]() not power valve and the intake has been re-torqued and it had some bolts that needed quite a bit
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65 Fastback 91 roller 306, H/C/I AOD-Bauman, PI Stallion, 4.10's and traction loc 04 Grand Cherokee Freedom Edition 79 Ford F-250 4x4 - Restored |
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#2 |
Ride Hard
Join Date: Oct 2000
Location: Wyoming IL
Posts: 1,094
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![]() So I thought I had it figured out, now I am not sure. However, I think I am chasing it down.
Decided to pull a plug, found that is was very black wit oil....dang it. This torques me off, cause I still have the plugs I ran in the E7TE's and they still look like new after two seasons.... Only three months old....maybe 1,000 miles. ![]() So then I pulled all the rest I can easily get to, all are black.... ![]() Just before peeps say it is a Ring or the short block.....negative....all 8 old plugs looked like this after two seasons of driving before my head swap ![]() So I was hoping it was intake gasket leak from hell, but doubt that even though I used the wrong washers on my intake. I am wondering if my freshly prepped heads by a local and reputable racing machine shop....dropped the ball and didn't really check my valve guides. To top it off, my neighbor came over and told me he has noticed a light smoke when I fire the car up here lately. any opinions? I am trying to figure out where I should go with this before I pull the heads for no reason. I already yanked the intake and I don't see any issues with leaks there. On a side note, right before I pulled it down, the problem was more pronounced even during a cold start up. I also checked the valve train, adjusted nicely already. thanks, Ryan
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65 Fastback 91 roller 306, H/C/I AOD-Bauman, PI Stallion, 4.10's and traction loc 04 Grand Cherokee Freedom Edition 79 Ford F-250 4x4 - Restored |
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#3 |
Registered Member
Join Date: Dec 2006
Location: new york
Posts: 482
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![]() you should do a compression test and see if u have a valve seat thats not true and are u sure ur push rods are the right size?also if u set the timming a few degrees higher does it go away?
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347 stroker all forged,arp everything,stud mains w/girdle,7qt pan,full roller, custom cam, aluminum heads swirl valves 5 angle valve job.quick fuel 750,areomotive pump,cobras w/nitto drags,and m/t et drags for the track, ford racing 373 gears,centerforce clutch,tko500,underdrive pulleys,bassani x-pipe,flowmasters ^best et so far 11.6 1.61 60ft coming soon 9sec et's ![]() 1992 mustang gt 2001 gmc 1500 4x4 78 century boat 92 skidoo |
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#4 |
Ride Hard
Join Date: Oct 2000
Location: Wyoming IL
Posts: 1,094
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![]() Don't know if the push rods are right, but I checked them myself when I ordered them, the right way. Car ran fine for 3 months, so I don't think that is it.
Can't check the other two things until I put the intake back on it ![]()
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65 Fastback 91 roller 306, H/C/I AOD-Bauman, PI Stallion, 4.10's and traction loc 04 Grand Cherokee Freedom Edition 79 Ford F-250 4x4 - Restored |
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#5 |
Ride Hard
Join Date: Oct 2000
Location: Wyoming IL
Posts: 1,094
|
![]() Just FYI, it was the Accel plugs. All is back and well again.
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65 Fastback 91 roller 306, H/C/I AOD-Bauman, PI Stallion, 4.10's and traction loc 04 Grand Cherokee Freedom Edition 79 Ford F-250 4x4 - Restored |
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