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#1 |
Registered Member
Join Date: Nov 2006
Location: Naples FL
Posts: 106
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![]() change all the plugs out again
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ZEX ![]() ![]() |
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#2 |
Registered Member
Join Date: Apr 2001
Location: Staging lane
Posts: 4,337
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![]() Yeah change the plugs again. If that doesnt work check the temp of the header tubes to find a potentially dead cylinder.
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92' LX-Big brakes, Lots and lots of suspension, GT40X heads, Ported cobra intake, stock cam, Vortech SC trim. 00' Lightning-Stock 88'CRX-13 second ego killer |
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#3 |
Registered Member
Join Date: Nov 2007
Location: OHIO
Posts: 20
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![]() Thanks for the direction guys. I work tonight so I'll try swapping out the plugs first thing in the morning.
By the way, do you think it's possible fuel would have gotten into the sensors through the vacuum lines and ruined them? like the MAP sensor and the rest that have vacuum lines attached? Thanks again, I'll let you know what I come up with. |
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#4 | |
Registered Member
Join Date: Apr 2001
Location: Staging lane
Posts: 4,337
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![]() Quote:
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92' LX-Big brakes, Lots and lots of suspension, GT40X heads, Ported cobra intake, stock cam, Vortech SC trim. 00' Lightning-Stock 88'CRX-13 second ego killer |
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#5 |
Registered Member
Join Date: Nov 2007
Location: OHIO
Posts: 20
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![]() This one was hydrolocked also, after the original regulator blew, before I changed plugs, when I took the old (original) plugs out, I turned it over in several short bursts and blew the fuel out of the cylinders, it was fuel. Yours was water?
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#6 | |
Registered Member
Join Date: Apr 2001
Location: Staging lane
Posts: 4,337
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![]() Quote:
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92' LX-Big brakes, Lots and lots of suspension, GT40X heads, Ported cobra intake, stock cam, Vortech SC trim. 00' Lightning-Stock 88'CRX-13 second ego killer |
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#7 |
Registered Member
Join Date: Nov 2007
Location: OHIO
Posts: 20
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![]() Well, I changed plugs out again, to no avail. EGR was bad, replaced it, as well as TPS, still not fixed. Noticed there were two vacuum solenoids on the right front inner fender on the the rear of the engine compartment that were damp with some gas, presumably from where the reg went bad and flooded the plenum and vacuum lines, I took them apart and cleaned them, that seemed to do the trick with getting the car running right and taking out the majority of the miss. But now I have severe idle surge, almost dropping to the point of killing itself, also running super rich. I've tried almost everything I can think of to narrow the problem down, but am having a heck of a time with it. Any ideas?
Keep in mind, I have just bought this car and don't have much idea about what mods previous owners have done to tune the car. |
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